Top Banner
Chamber Way Emergency Bridge Repair Bridge 5/227 ACEC/WSDOT Structures Meeting November 18, 2016
17

Chamber Way Emergency Bridge Repair Bridge 5/227 · Chamber Way Emergency Bridge Repair Bridge 5/227 ACEC/WSDOT Structures Meeting ... ACROW Span • Purchased by WSDOT • 50 ft

May 07, 2018

Download

Documents

LêHạnh
Welcome message from author
This document is posted to help you gain knowledge. Please leave a comment to let me know what you think about it! Share it to your friends and learn new things together.
Transcript
  • Chamber Way Emergency Bridge RepairBridge 5/227

    ACEC/WSDOT Structures MeetingNovember 18, 2016

  • Existing Bridge Built in 1958 4 simple spans, P.C. prestressed concrete girders SB min. clearance posted at 14-8 (Actual about 14-11) Bridge has been hit 9 times (known hits) Span 2: CL pier to CL Pier = 51-6

    Timeline Friday, July 22 - hit by unpermitted oversized truck Wednesday, July 27 AM damage span demolished Monday, August 1-2 50 ACROW span placed (approx. 51-0 end to end) Thursday, August 4 Built asphalt wedge ramps and open to traffic Mid October Sidewalk open to pedestrian traffic

    Chamber Way Emergency Bridge Repair

  • Chamber Way Emergency Bridge Repair

  • Chamber Way Emergency Bridge Repair

  • Chamber Way Emergency Bridge Repair

  • ACROW Span Purchased by WSDOT 50 ft 2 lane DS 24ft - w/ 5 ft footwalk DS = Double truss Single stack End to end length is approx. 51 ft

    Chamber Way Emergency Bridge Repair

  • Chamber Way Emergency Bridge Repair

  • Chamber Way Emergency Bridge Repair

  • Chamber Way Emergency Bridge Repair

  • Chamber Way Emergency Bridge Repair

  • Chamber Way Emergency Bridge Repair

  • Chamber Way Emergency Bridge Repair

  • Chamber Way Emergency Bridge Repair

  • Chamber Way Emergency Bridge Repair

  • Challenges: Open bridge timeline promises made to the public without checking with support teams Started construction of pedestals without signed plans

    o Constructed top of pedestal parallel to top of crossbeamo Required steel shims to level bearing plateo Bearing plate holes were not fields drilled to match anchor bolt patterno Used 40 ksi steel from Home Depot

    Started fabrication of steel members before field verifying bridge dimensionso Resulted in wasted material and re-fabrication of some members

    Delayed response to questions presented to project office o Resulted in rushed schedule at the end of design

    Designed twice with intent to speed delivery

    Chamber Way Emergency Bridge Repair

  • Public Relations Local economic impacts by cutting off access to retail (Walmart, Home Depot) Building relations with local agencies Showing good faith efforts to restore access for small communities

    Future Will be replaced with new 4-lane bridge Meet current minimum vertical clearance 16-6 Forward compatible with future corridor projects

    Chamber Way Emergency Bridge Repair

    Chamber Way Emergency Bridge RepairBridge 5/227Chamber Way Emergency Bridge RepairChamber Way Emergency Bridge RepairChamber Way Emergency Bridge RepairSlide Number 5Chamber Way Emergency Bridge RepairChamber Way Emergency Bridge RepairChamber Way Emergency Bridge RepairChamber Way Emergency Bridge RepairChamber Way Emergency Bridge RepairChamber Way Emergency Bridge RepairChamber Way Emergency Bridge RepairChamber Way Emergency Bridge RepairChamber Way Emergency Bridge RepairChamber Way Emergency Bridge RepairChamber Way Emergency Bridge RepairChamber Way Emergency Bridge Repair