Kochi Refinery BPCL –Kochi Refinery C.K. Soman DGM (Power & Utilities), BPCL KR Jaikishen C Nath SM(Power & Utilities), BPCL KR Challenges Faced & Lessons Learnt from the Commissioning and Stabilization of MS & HSD Quality up gradation Units
Kochi Refinery
BPCL –Kochi Refinery
C.K. Soman
DGM (Power & Utilities), BPCL KR
Jaikishen C Nath
SM(Power & Utilities), BPCL KR
Challenges Faced & Lessons Learnt from the Commissioning and Stabilization of MS & HSD Quality up gradation Units
Kochi Refinery
Growth Map of BPCL- KR through the years 2006-12
Challenges faced in bringing units online
Major failures during the initial phase
Learnings from the project
Road Map
Kochi Refinery
The Refinery that was; circa 2006
CDU 1 CDU 2 FCCU DHDS
GT 1 19MW STG 12MW GRID 4MW TOTAL 35MW
Kochi Refinery
The Capacity Expansion & Modernisation Project (CEMP II)
CDU 1 CDU 2 FCCU DHDS
GT 1 19MW STG 12MW GRID 4MW TOTAL 35MW
NHT CCR VGO DHS CDU2 Augmentation
Others
GT 2 34MW 220kV Yard 33kV &6.6kV levels
Kochi Refinery
Improve product quality to Euro III/ IV levels
Enhance refining capacity by 2MMTPA
Flexibility for further product quality up gradation
Objectives of the Project
Kochi Refinery
VGO-Hydro-desulphurisation (VGO-HDS) unit of 1.7 MMTPA capacity (M/s. UOP LLC, USA)
Continuous Catalytic Regeneration Reformer (CCR Reformer) of 0.85 MMTPA and Naphtha Hydro-Treater (NHT) Unit of 0.85 MMTPA capacity (M/s. UOP LLC, USA)
Revamp of Crude Distillation Unit II (CDU – II) from 3.0 MMTPA capacity to 5.0 MMTPA
100 TPH Utility Boiler, 72 TPH HRSG and matching offsite & other facilities
Process Units Added as part of CEMP II
Kochi Refinery
Addition of 34MW GTG
Augmented grid backup through 220kV substation
Replacement of obsolete 11kV Generation bus
33kV Distribution
6.6kV Utilisation
Changes in Electrical System
Kochi Refinery
220kV grid backup system slated for completion in first quarter of 2012
Load doubling to 60MW
New GTG in the commissioning stage
Process units commissioned ahead of power system elements
Challenges -Post CEMP II Electrical System
Kochi Refinery
Lin
k 2
KS
EB
2
KS
EB
1
ST
G
GT
1
Pre CEMP II Electrical Distribution System
Lin
k 1
11kV
11kV
66/11kV 66/11kV
Kochi Refinery
Load Growth Since Jan 2010
36 35
36 37 37
38 37
38
42 44
48 48
51 51
56 55
56
51
56
Jan
10
Fe
b 10
Ma
r 10
Ap
r 10
Ma
y 10
Jun
10
July
10
Au
g 10
Se
p 10
Oct 10
No
v 10
De
c 10
Jan
11
Fe
b 11
Ma
r 11
Ap
r 11
Ma
y 11
Jun
11
July
11
Plant load recorded Jan-10 to Jul-11
Peak load recorded Linear (Peak load recorded)
Kochi Refinery
Parallel operation was chosen for augmenting reliability
Or Run all the generators in parallel with the grid
Run the new units with power from the GTG being commissioned
Operation Philosophy
Kochi Refinery
VGO HDS,NHT
CCR,CDU2 New
Tie
4 T
ie 2
Tie
1
UTILITY,DHDS,
FCCU,CPP
AUX,CDU1 Lin
k 2
K
SE
B2
KS
EB
1
Te
mpora
ry L
ink
CDU2 Old, PRU,
ARU,PIBU, N/R,
Colony
ST
G
GT
1
GT
2
Lin
k 1
33kV,
25MW
HT 101
23MW
2101
11MW
Implementation of the chosen mode
Kochi Refinery
66kV grid backup designed for 20 MVA; other industries also fed from this line
Outage of New GTG, loads the grid lines to 28MVA approx
Load shedding turns off when in parallel
Old units also affected
Challenges -Post CEMP II Electrical System
GTG1
33%
GTG2
47%
STG
10%
KSEB IMPORT
9%TG
1%
Kochi Refinery
Shed the new units in tandem with the GTG outage to avoid overloading the grid lines
Utility systems to stabilise before the process units.
Tiding over and Learning
Kochi Refinery
Reliability issues faced
Revamp of old 11kV generation bus also included in CEMPII
BHEL commissions the panel as part of GTG package.
Flash over in May 2011
All units affected as the generator bus had tripped.
Kochi Refinery
Reliability issues faced
Flash caused by arcing of insulating material
Material found arcing even while meggering at 5000V.
Same material used all through, had to be removed
Kochi Refinery
Material issues and other rectifications to be addressed by BHEL during annual turn around
Concept of mixing revamps with unrelated projects to be reviewed
Tiding over and Learning
Kochi Refinery
Major Failures
Input transformer of RGC motor in CCR UNIT burnt.
6.6MVA transformer was supplied by Transfor, Switzerland
Kochi Refinery
Several teams were formed under an umbrella leadership.
Division of jobs coupled with group synergies of being under umbrella leadership brought back the plant by sourcing and commissioning a new transformer within a short span of 16 days.
Tiding over and Learning
Kochi Refinery
Commissioning and stabilisation of the power system elements like generators, substations etc to be completed prior to the process unit commissioning
The revamp and such other jobs not directly related to the main project but combined with it, shall be reviewed and monitored separately
Learnings in a Nutshell