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CEPSI2010_Parichart Remedial Action Step of Sub Synchronous Vibration _rev Oct 2010

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  • 8/8/2019 CEPSI2010_Parichart Remedial Action Step of Sub Synchronous Vibration _rev Oct 2010

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    TableIBearingDescription

    No. Type Diameter (Inches) Figure

    Bearingno.1

    DTP:DoubleTiltPadBearing

    (PivottedShoeJournalBearing,ButtonType,Pin

    Located,4Pads,1PadDown)

    fromKingsburyInc.

    12.018

    Bearingno.2 16.024

    Thiscombinedcyclepowerplant isconsistingof2GasTurbineand1SteamTurbineunits.TheSteamTurbine

    unitwasfirstsynchronized in1995andhadbeenexecutedwith5minorinspection(MI)and1majoroverhaul(MO)

    outages. TheSteam Turbine has been observed the symthom by condition monitoring which can be analyzed the

    trend simplyand speedily.The significantconditionmonitoringdatachosenareOverallShaftVibration,Admission

    SteamTurbineInletPressure,LPSteamTurbineInletTemperature,LPSteamExtractionTemperature,CondenserHighVacuumRangePressure,andLubeOilInletTemperature.TheOverallShaftVibrationisrecordedatbearinglocations

    andthesetpointacceptedbyGEcriteriaofalarmandtripis150 mppand225mpprespectively.

    OnMarch15th

    ,2008,thevibrationtrendpresentedasthefollowingfigurewasrecordedthetripeventwithout

    alarmsignalobservedbyoperator.ThiswasshowntheMVARs(GENVARS)decreasedfrom+10to 10when itwas

    broughtaGasTurbineunitdown.ThenSteamTurbinewas trippedby thevibration1X=230 mpp (2X=160 mpp)

    within20minutesafter.Moreover,thevibrationatBearingno.1(VIB1X,1YBRG#1)wasnotconsistencyobviously.

    TheSubsynchronousvibrationcouldnotbecapturedbyOverallVibrationmonitoring,so itwasneededtomeasure

    thespectrumvibration.

    Figure2VibrationtrendrecordofTripeventonMarch15th

    ,2008

    Pivoted

    shoe

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    METHODSAfter the tripeventwith230mpp, thevibrationanalyzing teamhad torecord theVibrationSpectrumofminutes

    before trip again. During testing, it was found that the Steam Turbine suddenly had vibrated up to the overall

    magnitudeof1X=134 mpp ,1Y=139mppat60MW (52% load)whenMVARchangedandabnormaldifferential

    expansionappearedasshowninthefigure3.Asshowninfigure4,theSubsynchronousof812Hzcapturedhadvalue

    upto10 mppandthenatthemomentoftripevent itsvalue increased immediatelyupto75mpp.Practicallythe

    normalSubsynchronoushadvaluednotover45 mppwhenaSteamTurbineisrunning.Therefore,thisproblemwasimpliedthatthepossiblecausescouldbefluidinducedinstability,theresultofBearingwear,Bearingoverclearance,abnormalofBearingAlignment.

    Figure3VibrationtrendrecordofTripeventonMarch17

    th

    ,2008

    Figure4SubsynchronousvibrationrecordoftestingonMarch17th

    ,2008

    Thehistoryrecordtoldusthatthevibrationhighproblemwasfoundsince2002.ItishighlyvibratedatBearingno.1

    during60MW(52%Load)whileanotherGasTurbinestartedupandSteamwasadmitted;however, Itcouldnotbe

    foundany severedamageonanybearings.Therefore,wekeptoncorrecting theproblemby lowspeedbalancing,

    field balancing, and bearing replacement depended on which obvious evidences found during such outages.

    Furthermore, the root cause analysis diagram in the below figure was the main tool to check the possible causes

    duringproblemsolving.

    Duringtheevent

    Beforetheevent

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    Figure4RootcauseanalysisdiagramofVibrationhighproblem

    Intheinitialcountermeasure,therewere2options,6dayworkingonCompromisedBalancingand8dayforBearing

    Inspection, in order to correct the problem. The 6day working including Generator preparation on Compromised

    Balancingwasselected.TheSteamTurbineandVibrationteamworkedtogethertoexecutethethreerunbalancing

    andanalyze thevibrationvectors, but the vibration stillhighat1x=200 mpp, instabilityofwhichhad resulted by

    Subsynchronousasusual.

    ThenwehadthemeetingagainandcomeupwithBearingInspectionfor8days.AftertheBearingno.1disassembly,

    the wear of pivoted shoe was shown in the figure 5, so the Bearing had to be replaced. As the following steps,

    Realignment (TurbineGenerator Coupling) had to be finished, as well as rubbing reducing by increasing oil seal

    clearance.

    Figure5ThepivotedshoeofBearingno.1Condition

    WhentheunitwasstartedupagainonApril12nd

    ,2008,itwasfoundthesamesignalthatwehadhavenbefore.

    However,theSteamTurbinewasabletosupplyhigherload,longerasitcouldrun.Inthemeanwhile,of90MW(78%

    Load)loadandtheVibrationatBearingNo.2shown130 mpp,theSteamTurbineteamtriedtoincreaseviscosityof

    inletlubeoilinorderthattheBearingmechanismwouldbeincreaseditsstiffness.Thetemperaturewasadjusted

    from49oCto46

    oC,buttheVibrationwasstillhigh.Thenthetemperaturewasbroughtbacktotheprevious.It

    eventuallytrippedatVibration2X=300 mpp(1X=220 mpp)whileMVARwasraised.

    Followingourexperiencestoresolvethisdifficulty,itcouldbesummarizedthatSubsynchronouscouldbeselfexcited

    from every single source of rotating behaviour such as Load exciting, Load increasing, MVAR increasing, Steam

    Admission,Startupmodeswitching,abnormaldifferentialexpansion,etc.TheSteampathwas likelytobeseriously

    clogged,soithadnosimpleremedyforseveraldays.Ifwecontinuedthecorrection,wewouldneedmoreinputdata

    SteamTurbineHighVibration

    AABBNNOORRMMAALL

    BBEEAARRIINNGG LLOOAADD

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    from theOEM (OriginalEquipmentManufacturer)Engineering,accuratehistoryrecord,besidesour technical team

    experiences.

    WithGErecommendations, Bearingboreswereadjustedandtherotorpositionwasmovedtoproperposition,butthe

    result was that the Steam Turbine was heavily vibrated at 5001,000 rpm. Consequently, the discussing meeting

    betweenthemanufacturer,GEanduser,EGAThadtheadditionalissueaboutgenerator2poleshortturnproblem.GE

    technicaladvisor(TA)recommendedthatthefirstprioritywasimprovingtheSteamTurbineconditiontobereadyto

    testrunforthegeneratorsolvingissue.

    Inthesummaryresultofthemeeting,itwasshownthatwecouldnotreducethevibrationwithoutSteamTurbineinternalpartcorrectionanymore.Hencethat45dayMajorOverhaulwasperformedtorehabilitatetheentireoftheSteamTurbinerotor. Infactofany

    unforeseen evidences enhancing Subsynchronous vibration, all parts of rotor obstructed the Steam path, working

    fluid,hadtobecloselytakencarebyGETAandEGATteam.

    Afterupperhalfcasing removal, the formeractivitiesperformedweredividing flange level inspection, frontcasing

    weightunbalancingtest(horndroptest),andBearinglevelcomparedwithdesignlevel.Theinspectionwasfoundthat

    theLeftsideofdividingflangelevelwaslowerthantherightsideof3mm.,69%offrontcasingweightunbalancing,andBearingno.1 level is lowerthandesignof2.7mils.Notonlywastheevidencefound,thewater inductiontrace

    alsoappeared.On June3rd

    ,2008, the front casingweightunbalancingwasadjusted tobewithin10%as shown in

    figure6,causingTurbinecasingLifting.Sothefollowingstepwas InternalAlignment,alldiaphragmstagecentering,

    andthelatteractivitiesarerubbingdecreasing,realignment,expandingtheanchorboltholes,Bearinginspectionand

    setting. In spite of foundation deformation found, the corrective action could not be done because of time

    constraints.Ithascontinuouslymonitoredtoprotecttheproblemintime.

    Figure6HydraulicliftingtheFrontcasingintheprocessofHorndroptest

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    Figure7WaterInductionDamageandRubbingRepairing

    Figure8ExpandingtheanchorboltholesofBaseplate

    Figure9BearingInspectionandSetting

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    RESULTSExecuting most of remedial action steps, we started up the unit again on July 20

    th, 2008. Notwithstanding

    Subsynchronousappearingofthe100MW(87%load),theTurbinecouldbearonhigherSubsynchronousmagnitude

    of80mppcomparedwith10mppoftheprevioustripevent.Infact,theSteamTurbineconditionwasbetter,butit

    furtherneeded fine tunning in thestartupprocessbyCompromisedbalancing tohandleTurbinecarefully.Because

    theBearingno.1 isverysensitive, itcanbestimulatednatural frequencyeasily.Thereforesuitableoilviscositywas

    adjustedbyinletLubricationoiladjustingtohelpsteadilyrotatablebearings.TheresultwasthattheSubsynchronousmagnitudereducedgradually.Itwasfirstlydecreasedfrom49

    oCto46.5

    oC,thentheSubsynchronouswasreduced as

    shown infigure10.Nextthetemperaturewasreducedto45oC,andtheSubsynchronouswasreduceddramatically.

    Finally,theunitcouldbebroughtbacktodispatchingcontrolcentertoThailandnationalelectricgridonAugust1st

    ,

    2008.

    Figure10TheSubsynchronous reducingfrominletLubeoiltemperatureAdjustingDuring2010minorinspectionoutage,wehadtoanalysebythepreviousrootcauseanalysisdiagramalongwiththe

    correctingactivitiesinoutage.Thelastpossiblecausewhichisabnormalbearingloadwasfoundbyanalysingtheshaft

    positionplotofallbearingpositions.ItwascorrectedbyliftingtheBearingno.3supporttodistributetheloadfrom

    Bearingno.2tootherbearingsandthentheSubsynchronouswasdisappearedcompletely.

    AccordingtotheexperiencesinSteamTurbineproblemanalysisandcorrection,mostlyinternalturbinepartcouldbe

    abletorepairinourEGATworkshop,soourteammustconsiderthemosteconomicaloptionwithtimeandmethod

    tradeoffdependingonourworkshopresourcesand teamcapabilities. Even though thechecklistof therootcause

    analysisfishbonediagramforthiscomplicatedproblemcouldbeapplied, inrealitywecounteredthebarriersduring

    countermeasureinsite.Themostimportantfactormustbeconsideredisselectingtherightmethodintherighttime.

    Forthisreason,theremedialactionstepofSubsynchronousvibrationtripcouldbesummarizedasfollowings.For Bently Nevada vibration monitoring system, this steam turbine is observed the rotating condition by Overall

    vibrationwhichhadthe150 mppand225 mppasalarmandTripsetpointsrespectively.

    IftheTripeventishappenedimmediatelyafteranymanuallyorautomaticallyprocessesoccur,measurethespectrum

    vibration and observe whether Subsynchronous is shown. If it is appeared, then indicate the magnitude of

    Subsynchronousvibration.TheprocessescanbeloadreducingbyshuttingdownoneofGasTurbine,loadincreasingbystartinguponeoftheGas

    TurbineandSteamadmission,MVARsraising,loadexciting,startupmodeswitching,etc.

    Incase,themagnitudeofSubsynchronousisnotover10 mpptobeartripevent.TheSteamTurbineconditionismost

    severe.TheinternalpartsofSteamTurbinehavetobeinspectedandcorrected.Checkthehorndroptestandcorrect

    ifneeded,centering,rubbingPartsreducing,Bearingsandpivotedshoesinspection,couplingalignmentetc.

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    In case, the magnitude of Subsynchronous is about 80 mpp to bear trip event. It is meant that Steam Turbine

    conditionisabnormal.Thereare3optionswithoutupperhalfcasingremovaltochoose.

    1. Adjustinginletlubricationoilfor12dayduringrunningCaution: Bearing metal temperature at other location might be high because of viscosity change, so it is

    neededcloselymonitoringduringadjustment.

    2. Compromisedbalancingfor6day:This isalsodependingon theposition to insertrequiredweights. If it isinsertedatTurbineGeneratorcoupling,thebalancingisonlyneeded2daycorrection.

    Caution:ThismethodwillsupporttheTurbinerunningatfull load,but itmightsuddenlyvibratedhighlyat

    75%load.Hencetheoperatorhastocarefullycarrytheturbinepassingthroughthisconditionsmoothly.

    3. Bearinginspectionfor8dayCaution:Thedisadvantageofthismethodisthatrealignmentduringhighturbinemetaltemperatureisquite

    difficult.

    Normally, if it does not have trip event, but the Subsynchronous signal sometimes appears during operation. The

    Steam Turbine Condition is quite normal. Keep monitoring the data: Bearing Metal Temperature, Lube Oil Inlet

    Temperature,Noiseat laststagebladeposition,BackPressure,StatorCoolingTemperature,MWandMVARChange

    comparedwithSubsynchronoustrend.RecordSubsynchronous andcomparewiththepreviousandpreparetoinspect

    andcorrectpossiblerubbingpartsand BearingsinspectionduringscheduledOverhaul.

    CONCLUSIONSIn Conclusion, the Subsynchronous vibration problem analysis needed to consider the entire area of rotating

    behaviour.TheEGATteamalsohadtomakedecisionundertimelimitandlesseffortrestriction.Moreover,themost

    importantbeforefollowingtheActionStep,theSteamTurbineconditionandaccuratemaintenancerecordhadtobe

    considered.TheobviousexampleisthatthefirstactionofCompromisedBalancingandLubeoiltemperatureadjusting

    wasnotsucceededbecauseoftheseriousdamagefromwaterinduction.Therefore,itprimarilyneededtocorrectall

    possiblerubbinginternalparts.

    ACKNOWLEDGMENTAsintheprevioussection,IhavereliedoncommentsandinformationfromanumberofengineerswithwhomIhave

    workedandcooperatedonanumberofprojectsoverthepastyears.Theircommentsandobservationshavebeenof

    considerable assistance in identifying areas where more detailed information is required and in bringing to my

    attention subjects that I may not havebeen, at that time, addressing in sufficientdetail,oreven atall. For these

    reasons,theirassistanceandadvicehasbeeninvaluable.

    As in this paper, my special thanks go to my colleagues Supaniti Songsawas, Manassavee Thuphom, and Cheewin

    Youngngern for allowing me to interrupt his work. Their review and input from their experience have added

    considerably toanyvalueotherplantengineersmayfindinthispaper.Theirconceptandthetimetakentoreadand

    commentonthetextandthewayithasbeenarrangedhavebeeninvaluable.

    Iwouldalso like toacknowledge the input from the followings.Eachhasmade informationavailable tomeorhas

    been prepared to discuss certain aspects of units and our joint experiences. Santhiti Chanthauthai, head of

    EngineeringSectioninSteamTurbineDepartment,SupawatKladthong,KobchaiWasuthalainan, ApichatPaugsopatai,

    Sompong Pantmuk of Steam Turbine Department, Sahathep Joipradit of other departments in Mechanical

    Maintenance Division, Pramote Kajornpol of South Bangkok Power Plant, EGAT, Athikom Jumrutsri, GE Technical

    Advisor.

    Tomakethetextclearer,Ihaveusedseveraloffiguresandtables.Someofthesewerepresentedatthepowerplant

    site,conferences,andseminarsIattended.

    Specialthanksgotomyofficestaff inSteamTurbineDepartment,fortheirassistance,especiallyWasuthepSinmayo

    andPhipobChomboonchoy.Theirhelpinparticularwasinvaluable.

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    REFERENCES[1] General Electric Company, Electrical Generating Authority of Thailand: South Bangkok Combined CyclePlant, South Bangkok, Thailand, File No. 62.1001 Steam Turbine Generator 103, Maintenance and SystemDescription,TurbineNo.270T238,GeneratorNo.290T238,Schenectady,NewYork:GE,1992[2] Grissom,B(2002),FundamentalsofRotatingMachineryDiagnostics,Minden,Nevada[3] H.P.Bloch,andM.P.Singh,SteamTubineSecondEdition:Design,applicationsand rerating, theUnitedStatesofAmerica,2009.[4] ElectricityGeneratingAuthorityofThailand,Rootcauseanalysisreport:SteamTurbineVibrationHighTrip,SBC10,Thailand,2008[5] Electricity Generating Authority of Thailand, Learning organization knowledge management report:RubbingCorrectionofSubsynchronousVibrationSteamTurbine,SBC10,Thailand,2008[6] GeneralElectric,SteamTurbineVibrationReport:ForcedOutageVibration,Thailand,2008

    Miss Parichart Suttiprasit obtained a Bachelors degree of Mechanical Engineering fromChulalongkornUniversity,Bangkok,Thailand in1999.SincejoiningElectricityGeneratingAuthorityof Thailand (EGAT) as a mechanical engineer in steam turbine department, she had carried outseveral works regarding problem solving on steam turbine operation and maintenance includingauxiliaries inEGATpowerplants.Currently,sheworksasaplanningengineer inbusinessplanningdepartmentofgenerationdeputy.Mr.ChaiyantTibdeeobtainedaBachelorsdegreeofMechanicalEngineeringfromSongklanakarin University, Hatyai, Thailand. In 1999, he initially worked as mechanical engineer in boilerdepartment;hehadcarriedoutseveralworksregardingproblemsolvingonboileroperationandmaintenance.Afterjoining the testingengineeringdepartment,heworksasamechanical testingengineerandhehasbeenexecutedmanyvibrationanalysistestingprojectsinEGATpowerplants.Mr.NaritWongsaobtainedahighvocationalcertificateinmechanicalareaandhasworkedassteamturbinesitemanagerinsteamturbinedepartment.SincejoiningEGATin1980,hehasexecutedalotof steam turbine outages in EGAT power plants as technical skill, foreman, and site manager.Regardingtohisworkexperiences,heexecutedtheissuesonsteamturbineandauxiliariessuchasproblemsolving,functiontesting,sitemanaging,etc.andhealsosuppliedthedetailsofthistopicinhisresponsibleareas.