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Best Practices in Energy Efficiency in Aluminium Smelting BEE Knowledge Exchange Platform 2015 Vedanta Smelter ,Jharsuguda
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Page 1: Best Practices in Energy Efficiency in Aluminium Smelting ... · PDF fileBest Practices in Energy Efficiency in Aluminium Smelting BEE Knowledge Exchange Platform ... of all air slide

Best Practices in Energy Efficiency in Aluminium Smelting

BEE Knowledge Exchange Platform – 2015

Vedanta Smelter ,Jharsuguda

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Entrepreneurship

Growth

Excellence Trust

Sustainability

VISION, MISSION & VALUES

VISION “We will be the world’s most admired company that consistently defines the leading standards in our businesses, making our stakeholders proud to be associated with us”

VALUES

MISSION “Our mission is to be a world class, diversified resources company that provides superior returns to its shareholders, through high-quality assets, low-cost operations and responsible corporate citizenship.”

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NATURAL RESOURCE-OUR BUSINESS

“Think Locally Act Globally”

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5 LTPA Aluminium Smelter 1215 MW CPP

12.5 LTPA Aluminium Smelter 2400 MW IPP

VEDANTA - JHARSUGUDA

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MAKING OF ALUMINIUM

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ALUMINIUM ELECTROLYSIS CELL

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ENERGY CONSERVATION

“Neither a campaign nor an initiative

It is our habit and culture”

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98%

2%

Electricity

Fuel

ALUMINIUM – ENERGY INTENSIVE

32%

68%

Energy

Other Cost

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ENCON PROJECTS (2011-14)

No. Of ENCON Projects

81

Energy Savings (M kWh)

385

Energy Savings (MT of fuel)

4020

INR Saving(Cr.)

112

INR Investment (Cr.)

3

“Small investments and high returns”

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MAJOR ENERGY SAVING PROJECTS

Sl.No. Title of the Project Energy Savings (MWh/Annum)

1 Reduction in Stub To Carbon voltage drop 109824 2 Reduction in Pot voltage . 62078

3 Improvement of current efficiency of pots. 45060

4 Implementation of slotted anode in pots 34330

5 Reduction of compressed air consumption. 19535

6 Reduction of dead pot voltage and crossover voltage .

8715

7 Optimization of Compressor running. 5310

8 Online addition of pots into circuit by fuse blown technology.

2324

9 HTM heater set point optimization in GAP. 1808

10 Reduction of the Specific Energy consumption of Wire Rod Mill. 1269

11 Improve Rodding shop availability. 589

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MAJOR FUEL SAVING PROJECTS

Sl.No. Title of the project Fuel Savings (MT/Annum)

1 Reduction of HFO consumption in Anode Baking Furnace

3051

2 Optimized usage of compressor in Metal Transport Vehicle

34

3 Reduction of diesel consumption in production vehicles by improving engine efficiency

27

4 Optimization of LPG burner use for ingot Casting.

15

“Save Today for a better Tomorrow”

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War Room Discussion

Asset Optimization Trophy

SMALL GROUP ACTIVITIES 2014-15

War Room

Project

Champions

Rectifier

• No. Of Projects : 4

• Yearly Saving : 355 MWh

• Employees:10

Utility

• No. Of Projects : 6

• Yearly Saving : 4082 MWh

• Employees : 8

Cast House

• No. Of Projects : 5

• Yearly Saving : 3791 MWh

• Employees : 25

Carbon

• No. Of Projects : 21

• Yearly Saving : 13087 MWh

• Employees : 120

Potline

• No. Of Projects : 6

• Yearly Saving : 184 MWh

• Employees: 200

Yearly Saving :- 22 M KWh

“We value every small Contribution”

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ENERGY CONSUMPTION TRENDS

45

50

55

60

2011-12 2012-13 2013-14 2014-15 TARGET

59 55 54 53.5 52.9

Total SEC-Smelter (GJ/MT)

HFO-Kg/MT

0

20

40

60

80

2011-12 2012-13 2013-14 2014-15 Target

70 64

54 48.2 45

HF0-Kg/MT

13400

13650

13900

14150

14400

14650

2011-12 2012-13 2013-14 2014-15 Target

14623

14024 13818 13806

13566

AC-KWh/MT

“Save What ?? Save a Watt”

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ENCON JOURNEY

2010

2011

2012

2013

Energy Audit by CII

Energy Audit by TERI

EnMS Implemented

ISO 50001 Certified CII Award

BEE Award

2014

GMEA award

CII Award

Russian Govt.- Award

NECA -1st Prize

Fuse Technology

Slotted Anode

Cathode

Clamp Drop

HFO & Stub to Carbon

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ENERGY OBJECTIVES 2015-2016

Reduce DC Energy Consumption from 13566 to 13322 KWh/Ton Reduce Auxiliary Energy Consumption from 397 to 382 KWh/Ton Reduce HFO Consumption from 48.2 to 45Kg/Ton

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REVIEW STRUCTURE

Formation of Energy Cell

Energy review structure

“Top to Bottom approach”

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IT ENABLEMENT

Energy Efficient Procurement

Capex Energy Impact Assessment

MES Online Flash Report

“Automation leads to Perfection”

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Magnetic Field Compensation Of Electrolysis Cells

18

Cathode Modification Of Electrolysis Cells

Up-gradation of Pot Control & Feeding System

ROAD MAP TOWARDS BENCHMARK

Waste Heat Recovery

“Measure to Control - Benchmark to Better”

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Cathode Modification

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CATHODE MODIFICATION

Savings/Year – 88 M KWh

Technical Invention Result (kWh/MT)

Change in Geometry of collector bar 76.8

Change in % of graphite in cathode block 60.8

Change in % of graphite in ramming paste 32.0

TOTAL ENERGY SAVINGS 169.6

“Every Unit counts”

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Reduction of HFO

Consumption

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PREHEATING CURVE MODIFICATION

RESULT • Preheating

temperature increased from 740°C to 800°C

• HFO injection reduced from 78 to 76 Hrs.

Preheating curve modified

to improve pitch volatile

combustion

300

400

500

600

700

800

900

0 2 4 6 8

10

12

14

16

18

20

22

24

26

28

30

Tem

per

atu

re (

°C)

Hrs

Pre Heating Curve Initial Final

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REDUCTION OF FALSE AIR INGRESS

Gap between burner stand & ring

Gap covered with packing coke

The gap between the flue and burner base ,flue hole cover , thermocouple base had false air intake

Effective sealing by Packing

Coke

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REDUCTION OF RADIATION LOSS BEFORE

• Flue Hole Covers were modified to reduce radiation losses

• Metallic cylinder and nets were replaced with ceramic wools and holding plates

• Insulation in the new design is farther from heat source • Cast Iron Rings were replaced by refractory rings • Redesigned covers surface temperature was lowered

by 73°C • Modified covers were Rs.700 cheaper than the original

design

AFTER

100

120

140

160

180

200

220

240

260

Before After

258

185

Cover Surface Temp.(°C)

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HFO consumption reduced from 63.8 to 46.6 kg/ MT of baked anode

Annual HFO Saving is 4800 MT resulting in cost saving of 20 Cr.

REDUCTION OF HFO CONSUMPTION

45

50

55

60

65

HFO CONSUMPTION KG/MT BAKED ANODE

“Improvement is an Infection”

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Reduction of Stub to

Carbon mV Drop

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mV

Carbon

Stub

Cast Iron

REDUCTION OF STUB TO CARBON mV DROP

Resistance at the gap filled by Cast

Iron between the Steel Stub & Carbon

Anode

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CAST IRON COMPOSITION

3.50

3.70

3.90

4.10

4.30

4.50

4.70

4.90

5.10

Apr/

13

Ma

y/1

3

Jun/1

3

Jul/13

Aug/1

3

Sep/1

3

Oct/13

No

v/1

3

De

c/1

3

Jan/1

4

Feb

/14

Ma

r/14

Apr/

14

Ma

y/1

4

Jun/1

4

Jul/14

Aug/1

4

Sep/1

4

Cast Iron Carbon Equivalent

Cast Iron C.E lsl usl

The contact resistance between Cast Iron & Carbon is a function of the Contact Pressure. The Contact Pressure is a function of Cast Iron Composition. The Carbon Equivalent of the Cast Iron was improved by Graphite addition instead of Amorphous Carbon

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STUB HOLE DESIGN CHANGE

The button at the bottom of the stub hole was removed to improve the contact pressure between Cast Iron & Carbon by reducing the air gap at the corners

BEFORE AFTER

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REDUCTION IN STUB TO CARBON mV DROP

Reduction in Stub to Carbon mV drop = 66 mV per Pot Savings/Year is 110 M KWh

mV 79

75

85

95

105

115

125

135

mV

Stub To Carbon mV Drop

“Every milli Volt Counts”

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Reduction in Cast Iron

Spillage

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Reduction in Cast Iron Spillage

Cast iron spillage during casting Cleaning and Re-melting it Spilled cast iron is 127 ton/month.

INTERVENTION:

Ladle Spout Modification. Cabin visibility improved Cleaning of bath from stubs

PROBLEM DEFINITION:

BENEFITS:

Cast iron spillage reduced by 87 ton/month.

Energy saved 0.7 M KWh/Year

12000 Man-Hours saved per year.

Total cost savings is Rs. 25 lakhs / year.

450mm

“Opportunity Everywhere”

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Cooling Fan Running

Hours

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We required higher draft to reduce HFO consumption which will increase power consumption.

We searched for opportunities to save energy.

INTERVENTION: Cooling fans stopped 4 Hours in every fire cycle

Energy consumption from 6912 KWH/day to

5760 KWH/day

Energy saving: 0.4 M KWh / Year

Cost saving: Rs. 10 lakhs / year

BENEFITS:

PROBLEM DEFINITION:

Baking Furnace Cooling Fans

“Conserve here to Consume there”

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Energy Reduction Billet

Homogenization

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PROBLEM DEFINITION: Power consumption in homogenizing furnace was

high at 220KWH/ton.

Replaced Rock wool to Rock wool + Cera wool sandwich

Power consumption reduced from 220 KWH/ton to 212 KWH/ton. Energy saved 1 M KWh/ year Cost savings is Rs. 25 lakhs/year.

INTERVENTION

BENEFITS

Energy saving in homogenizing furnace

“Kaizen for a Khazana”

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Reduction in ID Fan

Power Consumption

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PROBLEM DEFINITION: Power consumption of ID fan running with loading

of 16.82 MW.

ID fan loading reduced to 16.33 MW. Energy savings – 4.3 M KWh / Year Cost savings- Rs.1 Crore / Year

INTERVENTION

BENEFITS

Pot flow balancing. Hooding efficiency improvement Leakage reduction Improved gaskets for flange joints

Energy savings in FTP ID fan

16.2

16.3

16.4

16.5

16.6

Jan-15 Feb-15 Mar-15 Apr-15

ID FAN POWER CONSUMPTION(MW)

“Basics karo Bindass Raho”

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Coming Together is Business Thinking Together is Process Working Together is Success Keeping Together is Progress

“Bottom to Top Approach”

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Efforts towards GHG emission reduction :

Adoption of new technology. Stepping in towards renewable energy

sources. Creating awareness among employees and

stakeholders. Reduction in no. of light vehicle by

50%.Vehicle with aging less than 3 years only allowed & ensuring PUC certificate for every vehicle.

Increasing the load ability in transportation to reduce carbon emission

Inventory Mitigation

Year Scope 1 Emissions

CO2emission (MT)

Scope 2 Emissions

CO2 emission (MT)

Scope 3 Emissions

CO2emission (MT)

Total reduction in emissions intensity since baseline year study CO2e (MT)

FY 2012-13 (Base Year) 16330076 398 Not determined 16330474

FY 2013-14 15948488 2607 207040 15951095

CARBON FOOT PRINT ACTIVITIES

Drastic reduction of

2.3% from base year

(2012-13)

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HENCON & SIEMENS

OUR PARTNERS

Automation in cooling tower to control fan

switching in bake oven

Reactor Venturi modification and air

chamber plug modification of all air slide air chamber

in FTP

Automatic switching of

lighting circuit

Elimination of unwanted usage of compressor in

MTV

Checking of pressure

problem in MTV by using plant air

Energy saving- 0.7 M KWh/year

“Sabka Saath Sabka Vikash”

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Harnessing Solar Energy

Solar Water Evaporator

Eco Ventilators

Energy Saving – 5000 KWh/year

Solar Cell & LED

Lighting

RENEWABLE ENERGY SOURCES

“Future of Energy”

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Title Of The Project Potential Savings/Annum

1. Magnetic Field Compensation 324000 MWh 2. Cathode Modification

3. Up-gradation of Pot Control & Feeding System 4. Reduction of Compressed air consumption 4380 MWh 5. Use of High Density High weight anodes to reduce HFO & Energy consumption

360MT Carbon, 833 MWh, 220 MT HFO

6. VVFDs in fans and pumps 700 MWh

7. Reduction of HFO consumption by waste heat recovery 460 MT

8. Use of Solar Water Heater 120 MWh

9. Use of Energy Efficient Lights 83 MWh

10. Solar Photovoltaic Cell in administrative block. 60 MWh 11. Lighting energy savers in street lighting system. 31 MWh 12. Bio gas Plant for cooking in canteen. 1642 Kg

13.Waste Heat recovery from flue gases from BO & Potroom To Be Estimated

14. New Technology to reduce RO Rejections To Be Estimated

Our Plans For A Better Tomorrow….

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AWARDS & RECOGNITIONS

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Energy Conservation Category

National Award for the “Most Energy Efficient unit in

Aluminium sector” from honorable President of India.

Recognized as “Excellent Energy Efficient Unit” at 15th National

Award for “Excellence in Energy Management” organized by CII.

Sustainable Performance Category

Silver Category IMEA Award by Frost & Sullivan.

"Challengers Award - Mega Large Business" against "Frost &

Sullivan’s Green Manufacturing Excellence Awards 2014".

“Odisha EHS Award” by CII.

CSR award under two categories at “Odisha CSR conclave

2014”

Chairman’s Performance Award – Q1 , Q2 CY’13 & Q1, Q2

CY’14.

Sustainability Award – Winner in H2 & Runners up in H1 of

2013-14.

Engineering Excellence Award 2013 by Engineering Watch for

best innovation and engineering Marvel.

CPP has won 14th National Award For Excellent Energy Efficient

Unit-2013 By CII.

1st Prize for National Energy Conservation Award 2012 by

BEE.

International Green Apple Award for reduction in GHG

emission by introduction of slotted anodes for Smelter-I.

AWARDS & RECOGNITIONS

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"The more energy we save, the

more we save the next

generations"

“We are focussing on

renewable energy not for

laurels but to lighten homes

of the poor and bring a

change in their lives"

“Energy can be saviour of

generations”

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It takes

To transform

One will

A million

We harness our Collective will

Energy Conservation A Way of Life

To make

At Vedanta